{"id":4679,"date":"2024-03-06T10:44:43","date_gmt":"2024-03-06T01:44:43","guid":{"rendered":"https:\/\/www.dry-fog.com\/en\/?post_type=cases&#038;p=4679"},"modified":"2024-08-20T18:11:27","modified_gmt":"2024-08-20T09:11:27","slug":"hum-au-gravure","status":"publish","type":"cases","link":"https:\/\/www.dry-fog.com\/en\/projects-technology\/cases\/hum-au-gravure\/","title":{"rendered":"Revolutionizing Gravure Printing Processes: Safe and Energy-Efficient Humidification Solutions"},"content":{"rendered":"<h3>Reasons for Implementation<\/h3>\n<p>\u30fbThe rising costs of electricity and fuel highlighted the benefits of investing in switching humidification methods.<br \/>\n\u30fbThe demonstration convinced the customer of the feasibility of implementation.<br \/>\n\u30fbThe high return on investment facilitated seamless budget acquisition.<\/p>\n<hr \/>\n<h3>Challenges at a Gravure Printing Factory<\/h3>\n<p>The inks used in gravure printing processes contain highly volatile and flammable organic solvents, which are harmful when evaporated, thereby requiring a large volume of ventilation to refresh indoor air.<\/p>\n<p>On the other hand, ventilation that takes in outside air makes the indoor air dry, especially in winter, increasing the risk of fire caused by sparks from static electricity built up in the process. Furthermore, the dryness can cause airborne dust and particulates to adhere to the products, leading to quality failures. To address these issues, effective humidification equipment is essential in gravure printing factories.<\/p>\n<h3>Customer&#8217;s Initial Setup and Challenges<\/h3>\n<p>The customer who contacted us for solutions to these challenges had a boiler-based steam humidifier system already installed at their worksite. However, in their efforts to reduce CO2 emissions, they were facing issues with the steam humidification, which requires heat for its operation, leading to high fuel and electricity consumption and increased CO2 emissions. Additionally, the recent rise in electricity and fuel costs has become a significant concern.<\/p>\n<p><img decoding=\"async\" loading=\"lazy\" src=\"https:\/\/stg.dry-fog.com\/en\/wp-content\/uploads\/sites\/3\/2024\/03\/gravure-article-02.jpg\" alt=\"\" width=\"1536\" height=\"852\" class=\"alignnone size-full wp-image-4725\" srcset=\"https:\/\/www.dry-fog.com\/en\/wp-content\/uploads\/sites\/3\/2024\/03\/gravure-article-02.jpg 1536w, https:\/\/www.dry-fog.com\/en\/wp-content\/uploads\/sites\/3\/2024\/03\/gravure-article-02-300x166.jpg 300w, https:\/\/www.dry-fog.com\/en\/wp-content\/uploads\/sites\/3\/2024\/03\/gravure-article-02-1024x568.jpg 1024w, https:\/\/www.dry-fog.com\/en\/wp-content\/uploads\/sites\/3\/2024\/03\/gravure-article-02-768x426.jpg 768w, https:\/\/www.dry-fog.com\/en\/wp-content\/uploads\/sites\/3\/2024\/03\/gravure-article-02-699x388.jpg 699w, https:\/\/www.dry-fog.com\/en\/wp-content\/uploads\/sites\/3\/2024\/03\/gravure-article-02-540x300.jpg 540w, https:\/\/www.dry-fog.com\/en\/wp-content\/uploads\/sites\/3\/2024\/03\/gravure-article-02-220x122.jpg 220w\" sizes=\"(max-width: 1536px) 100vw, 1536px\" \/><br \/>\nSwitching from boiler-based steam humidification to other methods for energy savings.<\/p>\n<div style=\"max-width:1100px;text-align:center;margin: 4rem auto 8rem\">\n<div>\n<a style=\"margin-bottom:1rem;justify-content: center;align-items: center;padding: 1.5rem 6rem;color: #fff;font-weight: 500;font-size:1.2rem;float: left;margin-left:10px;width:auto;background: linear-gradient(20deg, rgba(31,207,158,1) 0%, rgba(27,217,168,1) 35%, rgba(19,222,173,1) 100%);border-radius: 3px\" href=\"https:\/\/www.dry-fog.com\/en\/documents\/report\/\" target=\"_blank\" rel=\"noopener\">View All Case Studies<\/a>\n<\/div>\n<div>\n<a style=\"margin-bottom:1rem;justify-content: center;align-items: center;padding: 1.5rem 9rem;color: #fff;font-weight: 500;font-size:1.2rem;float: left;margin-left:10px;width:auto;background: linear-gradient(20deg, rgba(31,207,158,1) 0%, rgba(27,217,168,1) 35%, rgba(19,222,173,1) 100%);border-radius: 3px\" href=\"https:\/\/www.dry-fog.com\/en\/contact\/\" target=\"_blank\" rel=\"noopener\">Contact Us<\/a>\n<\/div>\n<\/div>\n<div style=\"clear:both\"><\/div>\n<h3>Innovative Proposal from IKEUCHI<\/h3>\n<p>Switching from the steam humidification to the water spray humidification we proposed required maintaining a relative humidity of 50% around the ink units, where sparks tend to arise.<\/p>\n<p>To achieve this, we selected the AirULM, which was expected to deliver the highest energy-saving performance under the given conditions, from our three system products\u2014AirHybrid, AirAKI, and AirULM\u2014and then proposed the &#8220;spot humidification&#8221; approach by installing the explosion-proof AirULM headers at positions close to the ink units.<\/p>\n<h3>Cost-Effective Spot Humidification<\/h3>\n<p>Spot humidification allows for humidity increases at targeted spots, significantly suppressing operating costs compared to the approach of maintaining stable humidity levels across the entire floor.<\/p>\n<h3>Customized Installation for Optimal Results<\/h3>\n<p>We tailored the header to the length of the printing process line, installing eight nozzles on a 4-meter header. This setup achieved the target condition with approximately one-third to one-half of the total humidification volume required for the entire floor.<br \/>\nFurthermore, by conducting an on-site demonstration, we provided the customer with a hands-on experience, helping them visualize the implementation and understand the cost-effectiveness beforehand.<\/p>\n<p><img decoding=\"async\" loading=\"lazy\" src=\"https:\/\/stg.dry-fog.com\/en\/wp-content\/uploads\/sites\/3\/2024\/03\/gravure-article-01-1.jpg\" alt=\"\" width=\"1536\" height=\"916\" class=\"alignnone size-full wp-image-4728\" srcset=\"https:\/\/www.dry-fog.com\/en\/wp-content\/uploads\/sites\/3\/2024\/03\/gravure-article-01-1.jpg 1536w, https:\/\/www.dry-fog.com\/en\/wp-content\/uploads\/sites\/3\/2024\/03\/gravure-article-01-1-300x179.jpg 300w, https:\/\/www.dry-fog.com\/en\/wp-content\/uploads\/sites\/3\/2024\/03\/gravure-article-01-1-1024x611.jpg 1024w, https:\/\/www.dry-fog.com\/en\/wp-content\/uploads\/sites\/3\/2024\/03\/gravure-article-01-1-768x458.jpg 768w, https:\/\/www.dry-fog.com\/en\/wp-content\/uploads\/sites\/3\/2024\/03\/gravure-article-01-1-651x388.jpg 651w, https:\/\/www.dry-fog.com\/en\/wp-content\/uploads\/sites\/3\/2024\/03\/gravure-article-01-1-540x322.jpg 540w, https:\/\/www.dry-fog.com\/en\/wp-content\/uploads\/sites\/3\/2024\/03\/gravure-article-01-1-220x131.jpg 220w\" sizes=\"(max-width: 1536px) 100vw, 1536px\" \/><br \/>\nThe nozzle used with the AU header producing a very fine fog with a mean droplet diameter of 20 to 30 \u00b5m.<\/p>\n<div style=\"max-width:1100px;text-align:center;margin: 4rem auto 8rem\">\n<div>\n<a style=\"margin-bottom:1rem;justify-content: center;align-items: center;padding: 1.5rem 6rem;color: #fff;font-weight: 500;font-size:1.2rem;float: left;margin-left:10px;width:auto;background: linear-gradient(20deg, rgba(31,207,158,1) 0%, rgba(27,217,168,1) 35%, rgba(19,222,173,1) 100%);border-radius: 3px\" href=\"https:\/\/www.dry-fog.com\/en\/documents\/report\/\" target=\"_blank\" rel=\"noopener\">View All Case Studies<\/a>\n<\/div>\n<div>\n<a style=\"margin-bottom:1rem;justify-content: center;align-items: center;padding: 1.5rem 9rem;color: #fff;font-weight: 500;font-size:1.2rem;float: left;margin-left:10px;width:auto;background: linear-gradient(20deg, rgba(31,207,158,1) 0%, rgba(27,217,168,1) 35%, rgba(19,222,173,1) 100%);border-radius: 3px\" href=\"https:\/\/www.dry-fog.com\/en\/contact\/\" target=\"_blank\" rel=\"noopener\">Contact Us<\/a>\n<\/div>\n<\/div>\n<div style=\"clear:both\"><\/div>\n<h3>Benefits of Implementation<\/h3>\n<p>Halting the use of the boiler-based steam humidification has resulted in substantial energy savings, allowing the initial investment to be recouped in about one year.<\/p>\n<p>The steam humidification, which also caused the worksite temperature to rise, posed a significant burden on the employees working in uniform. However, with the new system, they have reported that it became cooler, and the worksite environment has improved.<\/p>\n<h3>Ensuring Safety and Promoting Sustainability<\/h3>\n<p>Switching from the steam humidification to the water spray not only ensures safety by reducing fire risks associated with organic solvents and static electricity but also promotes environmental friendliness and energy savings, furthermore contributing to establishing a more comfortable working environment.<\/p>\n<h3>Commitment to Continuous Improvement<\/h3>\n<p>IKEUCHI remains committed to addressing on-site challenges in printing factories.<\/p>\n","protected":false},"featured_media":0,"template":"","cat_cases":[88],"tag_cases":[411,352,350,349],"acf":[],"_links":{"self":[{"href":"https:\/\/www.dry-fog.com\/en\/wp-json\/wp\/v2\/cases\/4679"}],"collection":[{"href":"https:\/\/www.dry-fog.com\/en\/wp-json\/wp\/v2\/cases"}],"about":[{"href":"https:\/\/www.dry-fog.com\/en\/wp-json\/wp\/v2\/types\/cases"}],"wp:attachment":[{"href":"https:\/\/www.dry-fog.com\/en\/wp-json\/wp\/v2\/media?parent=4679"}],"wp:term":[{"taxonomy":"cat_cases","embeddable":true,"href":"https:\/\/www.dry-fog.com\/en\/wp-json\/wp\/v2\/cat_cases?post=4679"},{"taxonomy":"tag_cases","embeddable":true,"href":"https:\/\/www.dry-fog.com\/en\/wp-json\/wp\/v2\/tag_cases?post=4679"}],"curies":[{"name":"wp","href":"https:\/\/api.w.org\/{rel}","templated":true}]}}